I was running my Maxx with the DYN big block conv. this afternoon and my motor HPI .25 started to bog real heavy so like true warrior I pulled the gas even harder and that was it. It stopped and seized up and when I took it apart the bottom of the connecting rod had blown out. The crank was ripped out of the hole. WHat do you think caused this? It was a motor I got used through a trade not a big deal but I've been racing 1/8 for 6 year and have never seen nothing like this before.